Quote from: woods170 on 09/23/2016 07:03 pmIMO the only part of the high pressure helium system that has the energetic potential to pop the upper stage in less than 1/10th of a second is a pressurized COPV letting go.The strut incident destroyed the second stage in flight. If we believe the strut was at fault, a COPV failure was not needed to breech the the second stage.Matthew
IMO the only part of the high pressure helium system that has the energetic potential to pop the upper stage in less than 1/10th of a second is a pressurized COPV letting go.
Quote from: guckyfan on 09/23/2016 05:44 pmThey still want to fly again in November which sounds optimistic.Yeah. I would estimate 6 to 9 months if it's a quality control issue, 9 to 12 month if they have to redesign something or fabricate a long lead item.
They still want to fly again in November which sounds optimistic.
People keep saying COPV. The SpaceX statement doesn't say "COPV". It says "cryogenic Helium system". There is way more to this system than just the tanks (and the struts that support them.) There is lots of piping, valves, regulators, and a supply system from the TEL.Edit: correct quote from SpaceX
Quote from: matthewkantar on 09/23/2016 07:22 pmQuote from: woods170 on 09/23/2016 07:03 pmIMO the only part of the high pressure helium system that has the energetic potential to pop the upper stage in less than 1/10th of a second is a pressurized COPV letting go.The strut incident destroyed the second stage in flight. If we believe the strut was at fault, a COPV failure was not needed to breech the the second stage.MatthewThe difference was the the CRS-7 stage didn't disintegrate suddenly, as did this one. - Ed Kyle
I'm not sure. Couldn't a burst in the high pressure plumbing responsible for charging up those COPVs result in a breach in the common bulkhead of sufficient energy to allow enough mixing between LOX and RP-1 and make a nice boom?
Quote from: Jim on 09/23/2016 07:13 pmQuote from: John Alan on 09/23/2016 07:07 pm.The flash was chunks of the fitting going thru the side of the tank and the AL/LOX flash fire that resulted...It was a RP-1/LOX fire, not ALCall it RP-1/LOX/AL fire then... my opinion...
Quote from: John Alan on 09/23/2016 07:07 pm.The flash was chunks of the fitting going thru the side of the tank and the AL/LOX flash fire that resulted...It was a RP-1/LOX fire, not AL
.The flash was chunks of the fitting going thru the side of the tank and the AL/LOX flash fire that resulted...
Quote from: SWGlassPit on 09/23/2016 07:06 pmI'm not sure. Couldn't a burst in the high pressure plumbing responsible for charging up those COPVs result in a breach in the common bulkhead of sufficient energy to allow enough mixing between LOX and RP-1 and make a nice boom?This has been a hunch of mine from the get go, especially since the tanks in theory weren't completely filled yet.
Quote from: John Alan on 09/23/2016 07:18 pmQuote from: Jim on 09/23/2016 07:13 pmQuote from: John Alan on 09/23/2016 07:07 pm.The flash was chunks of the fitting going thru the side of the tank and the AL/LOX flash fire that resulted...It was a RP-1/LOX fire, not ALCall it RP-1/LOX/AL fire then... my opinion... Not Data supports that claim
Anyone of those changes is IMO going to eat into F9's performance.
Quote from: ccicchitelli on 09/23/2016 07:42 pmQuote from: SWGlassPit on 09/23/2016 07:06 pmI'm not sure. Couldn't a burst in the high pressure plumbing responsible for charging up those COPVs result in a breach in the common bulkhead of sufficient energy to allow enough mixing between LOX and RP-1 and make a nice boom?This has been a hunch of mine from the get go, especially since the tanks in theory weren't completely filled yet. If there was a break in the plumbing of the He system, that was immersed in the subcooled LOx and the gaseous He was at a temperature that would help flash the subcooled LOx to a gas to a vapor it would have a multiplier affect on over pressuring the tank.There are enough brains on the investigation that they could crunch through the numbers on the level of LOx, initial tank pressure, burst pressure and how much much of a flow rate of He would have been needed to burst in the less than 93 milliseconds.The COPVs maybe fine, it wasn't the COPV that failed on CRS-7, it was the strut and in this case it may not be the bottle either. Immersing a system into a subcooled cryogenic system may need to be revisited however.
I support that statement. LOX & Al fire is bright white due to extreme temperature. Also a lot of white smoke gets produced. This is completely unlike the relatively low temperature combustion that we saw.
When I first read that update on Twitter, my initial thought was damn it, Jim was right. But just from re-reading the wording, I'm not convinced the COPV did pop, perhaps like was written above it was a fitting or some other piece of the plumbing. IF it really was the COPV failing, it's hard for me to believe that the November time frame would even be discussed.
IDK if this includes or excludes GSE or TEL malfunctions. It does say "of the..." not "in the..." so the focus could be ambiguous
Quote from: wannamoonbase on 09/23/2016 07:55 pmQuote from: ccicchitelli on 09/23/2016 07:42 pmQuote from: SWGlassPit on 09/23/2016 07:06 pmI'm not sure. Couldn't a burst in the high pressure plumbing responsible for charging up those COPVs result in a breach in the common bulkhead of sufficient energy to allow enough mixing between LOX and RP-1 and make a nice boom?This has been a hunch of mine from the get go, especially since the tanks in theory weren't completely filled yet. If there was a break in the plumbing of the He system, that was immersed in the subcooled LOx and the gaseous He was at a temperature that would help flash the subcooled LOx to a gas to a vapor it would have a multiplier affect on over pressuring the tank.There are enough brains on the investigation that they could crunch through the numbers on the level of LOx, initial tank pressure, burst pressure and how much much of a flow rate of He would have been needed to burst in the less than 93 milliseconds.The COPVs maybe fine, it wasn't the COPV that failed on CRS-7, it was the strut and in this case it may not be the bottle either. Immersing a system into a subcooled cryogenic system may need to be revisited however. If any part of the helium system failed under pressure, see this comment about how fast loose or fragmenting things would try to move (ignore the FAE commentary. Not needed):http://forum.nasaspaceflight.com/index.php?topic=30981.msg1583947#msg1583947Remember your kinetic energy formula to find the energy for anything that's moving as a result of the failure to get up to ignition temperature: KE = 1/2 (M * (V * V)) in one video frame time you can easily get 15 feet of object motion for bashing, mixing and booming. You don't need a lot of mixed RP1 & LOX to get that boom started as seen in frame 1.IMHO whatever happened after the "system failed under pressure" was really really fast.The claim that they have 90 ms of data prior to loss of data would suggest to me that they would have 75 or more ms of data of whatever lead up to the event, assuming the data loss occurred within 16 ms of the breach.What is intriguing to me is 90 ms is a long time, the last 5 frames in the USLR video don't show anything unusual, but could be covering the time line from onset to failure.
Quote from: wtrix on 09/23/2016 08:15 pmI support that statement. LOX & Al fire is bright white due to extreme temperature. Also a lot of white smoke gets produced. This is completely unlike the relatively low temperature combustion that we saw.Still unsupported. And you are just basing it from one camera view. The camera just was over saturated and no smoke but white vapors.
There's no reason to assume that happened simultaneously with the tank breach.
Quote from: mme on 09/23/2016 06:17 pmOn the other, I think that if they had any level of confidence that a specific failure was the root cause they would have mentioned that in their update.That isn't the way PR works. You say just enough to update folks, but not get ahead of the investigation team. There is a reason Elon isn't out their tweeting updates to the same extent like the last time (CRS-7). He is learning to let his communication team take the lead. They will finalize the results when the official report comes out. From the sound of it, that could be in the next couple months. If RTF November/December is really in the cards.
On the other, I think that if they had any level of confidence that a specific failure was the root cause they would have mentioned that in their update.